Wednesday, June 5, 2013

Mill: Gibs

Please read the complete article:
http://benchtopmachineshop.blogspot.com/2017/04/mill-gibs.html


I think the gibs which come with the mill are fine, except the divots for the set screws are woefully inadequate. Because the set screws aren't pushing against a flat, they tend to rotate the gib, which compromises rigidity and creates uneven wear.



To fix this I decided to machine proper flats into the gibs for the set screws to sit on. First I removed all the set screws for the gib, then installed and positioned the gib. I sharpened the end of two M4 set screws in my lathe and first installed one and tightened it down, and then tightened the other one in each hole in turn. This left exact center marks for all the set screws. From measurements it looks like the gib angle is 55*, so I used my Wixey angle gauge to set my angle vise. Since the gib wanted to rotate when the vise was tightened, I placed a section of 1/2" steel rod in the corner formed by the gib and vise jaw, and then used my table clamp set to push down on the rod, effectively locking the gib in place. I then machined the flats using a 3/16" end mill with a plunge cut. For the lock's flat I used a 1/4" end mill.  By the way, that gouge you see is what happens when your vise decides to let go of the work.



The set screws were also upgraded from the stock dog point to cup point. The last couple millimeters of the set screws were turned down so they just fit in the gib pocket. This helped position the gib horizontally and keep it from sliding on the set screws.

I also took the opportunity to lap the gib slightly, but it turned out it was pretty flat to begin with. Once everything was reassembled, the gib has much more contact with the dovetail, and I can tighten the set screws tighter without making it hard to move. It was well worth it in my opinion.

I didn't like how the gib locks looked either. They have a rounded nose which pretty quickly becomes deformed through use. 



I figured if they had a flat nose to push against a flat surface, they'd work a lot better and wouldn't deform. So it was disassembled and thrown in the lathe where its end was extended and faced flat. Since its end turns on the gib I greased it just before assembly.


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